Update #2 of 19-20 NURC
- dvhsunderwaterrobotics
- Nov 27, 2019
- 1 min read
Welcome back to our page!
What we've been working on these past weeks is creating a new layout of 6 motors instead of 4 for the sub and testing

Compared to 4 motor set up


Unfortunately during testing our ground wire in the USB became unsoldered and ended up snapping making us have to take Castellious 2.0 apart so close to when it had been put together.


Hope to see you again soon,
-Head of Logistics
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